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Remove brushless DC motor commutation spikes

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Successful removal of the excessive current and consequent back emf present at the end of the commutation period for a brushless DC motor results in improvements in efficiency, reduced component cost and lower acoustic noise. A technique of ‘tail-end’ current control integrated within a motor pre-driver IC provides a solution that supports existing half and full-bridge speed control circuitry. The significance of excessive current is clearly illustrated in Figure 1.

typical_blcd_motor_supply_current_waveform

At the start of the commutation cycle, when the currents are fi rst switched on in the coil, rotor and stator are of the same polarity, so repel each other in the desired direction of rotation. At this time the current in the coil quickly rises and then levels off to a peak at approximately one quarter of the way through the commutation cycle after which point it starts to fall slightly to around 90% of the peak value at around three quarters of the way through the cycle. After this low there is then a sharp rise in current flow to a level above that of the first peak. At this point the commutation takes place, at the worst possible time where the current is at its peak value. The switching of the coil results in a large back emf voltage across the now open circuit coil resulting in a number of undesirable effects within the motor and its electronics. Most notable is the charge-pump effect the voltage has within the motor when a reverse protection diode is present. This is illustrated in Figure 2 for a typical H-bridge configuration for a single-phase BLDC motor.

attempted_current_path

Current practice
A number of methods are used to compensate for these effects. One method is to over-specify the power switching devices driving the coil. This enables them to withstand the severe voltages and currents generated as a of such overly robust components generally results in a more expensive solution than should be the case. A disadvantage of over-specifying the voltage rating of the power devices is that for each doubling of the voltage rating of the device, the RDS(on) - in the case of MOSFETs - will also double, resulting in higher power dissipation in the devices. To help reduce the voltage ‘spike’ a capacitor is included in the electronics across the power driving circuit to dampen the over-voltages present. While this has a beneficial effect in that energy is saved in the capacitor to improve efficiency, it again adds cost. The damping effect is shown in Figure 3.

capacitor_effects_emf

Another method to restrict the excessive end of commutation current flow is to advance the Hall device, in conjunction with a large commutation delay time, so that commutation takes place before the current reaches too high a value. Too much advance, however, and the motor becomes difficult to start, so there does become a limit to what can be achieved. A further method is to introduce some form of current control in the motor to ‘clip‘ the current peak. This latter method also has an undesirable effect, in that it can restrict the initial current peak where most of the torque is generated. Although any combination of the methods described above can be used, it will be apparent that all are reactive to the effects, rather than being proactive at removing the root cause of the problem of the switching of the high currents at the end of the commutation cycle.

Tail-end current control
In the early part of the commutation cycle, when the poles of the rotor and stator are the same polarity, there is considerable work done as the two poles repel each other and are attracted to the neighboring poles. It is in this early stage that most of the torque is generated. However, towards the end of the commutation cycle, as the opposing poles become increasingly aligned as they are attracted to each other, there is less and less torque being generated and yet the current flow in the coil is becoming increasingly excessive. This excessive current needs to be kept under control to improve efficiency and to reduce the need for using over specified components. However, use In order to control the speed of brushless DC motors, pulse width modulation (PWM) is increasingly being used to switch the coil on and off at a high frequencies. This varies the amount of energy in the coil. The PWM is also used to control the peak currents as described previously. This PWM control circuitry is already integrated into the controller for speed control purposes and therefore lends itself as an ideal method for controlling the current flowing in the coil towards the end of the commutation cycle. The technique, therefore, is to use the PWM to slowly ramp down the current, from the low level at the 75% point of the commutation cycle, to zero current flow by the end of the commutation.

Methodology
The PWM circuit within the motor controller is stimulated by a voltage control signal. A high voltage will provide 0% PWM and a low voltage 100% PWM. Changing between these high and low voltages provides a variable amount of PWM drive that is proportional to the input control voltage. In order to apply a current reduction signal to the end of the cycle when a motor is running, we first need to know the motor speed. An integrator therefore becomes one of the first building blocks in the new system. A triangular waveform is also generated as a voltage vs. commutation period signal. The integrated and triangular waveforms are then combined to
provide a third signal to modulate the PWM control voltage.

Results
The resultant supply current waveform is shown in Figure 4. Here the shaping of the current waveform can be clearly seen. This plot, when compared with that in Figure 1, quickly shows the removal of the high current ‘spike’ at the end of the commutation cycle. The disturbance on the supply, while not illustrated here, is also removed to zero. This evaluation was conducted on a fan running at around 7500rpm and drawing 0.8A. Table 1 shows the results attained using the same fan motor, first with no modification and then again after inclusion of current control at the end of the commutation cycle. It can be seen that the current has dropped by 16%, however, the speed has only dropped off by 6%, giving a considerable improvement in the overall motor efficiency. Tests conducted on another motor produced a current drop of 10% and a speed drop of 2%. This small loss in speed will be more than compensated for by enabling the use of lower voltage MOSFET devices with a lower RDS(on).

Advantages
As this technique reduces the excessive current flow in the most inefficient part of the commutation cycle, it has an immediate knock-on effect on efficiency. As described, 10% reduction in current consumption has been achieved with a minimal, and in other cases, zero reduction in speed. Refinement of the technique should see improvements beyond this. The resulting ability to keep to a realistic voltage rating for the components also reduces the internal motor dissipation, most welcome in the cramped conditions inside a BLDC motor.
Finally, as the current waveform generated by this new technique is more sinusoidal, the movement of the stator plates becomes quieter, thus reducing high speed commutation noise.

Source: Technology First

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